Jasonpatrick
Friend of Leo's
Which ballpark? Seems to be a few hahaI use a 5V4 in my clone and it gets it "in the ballpark".
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Which ballpark? Seems to be a few hahaI use a 5V4 in my clone and it gets it "in the ballpark".
Between 60 and 70% dissipation and voltage near or below 400v.Which ballpark? Seems to be a few haha
The negative bias voltage is also listed as -26. This may be a mistake on their part, as at that setting, the power tubes would run very, very hot, which would also drop the plate voltage.That is surprising.
You have your power tube plate voltage well above the schematic value, 365V, but the pre amp voltage match the schematic.
I know fender schematics need some interpreting, but that is hard to make sense of.
Nothing to worry about however.
Another option would be to replicate the current draw of the missing normal channel input stage by adding a resistor of about 270k to 330k between B+4 and ground.I’m on the fence about upping the last dropping resistor from 27k to 47k since I’m missing a tube or even maybe looking at the 10k and making it a 22k but you let me know what you all think
You rock. Great idea !Another option would be to replicate the current draw of the missing normal channel input stage by adding a resistor of about 270k to 330k between B+4 and ground.
That should keep the time constants in the HT supply about the same as stock.
So AnB w/270k and without. It dropped the voltages a bit. V1 is down to 167 and 184 pin 1-6. bias also dropped on both, now they are 1.4 and 1.36. B+4 is now 286vdc. PI voltage changed a little, now 256v and 251v. Everything else dropped a volt or less. Sounds great. Maybe a tad better? lol I doubt it. Probably all in my head. Thanks for the suggestion. Learned something new today.Another option would be to replicate the current draw of the missing normal channel input stage by adding a resistor of about 270k to 330k between B+4 and ground.
That should keep the time constants and voltages in the HT supply about the same as stock.
Food for thoughtsMy G63 clone uses the Weber W130something "Deluxe power transformer" of Chinese origin. I was pleased that when I chose the lower 275volt secondaries and genuine British GZ34 I ended up with 375VDC of B+. But if yours is too high, that's where a 5V4 would come in handy
Just rechecked out of curiosity. 390 volts at just about 20ma. That's around 60% for 14 watts, or just under 70% for 12 watts.Between 60 and 70% dissipation and voltage near or below 400v.
The negative bias voltage is also listed as -26. This may be a mistake on their part, as at that setting, the power tubes would run very, very hot, which would also drop the plate voltage.
I've yet to see any 6G3 that matches the plate voltage on the schematic (365V). That said, my amp used the 125P2A and using the stock GZ34 it ran the power tubes in the 448v range, biased at 20mA per tube. The pre-amp voltages were also higher.That’s why I said that it is hard to make sense of your power tube plate voltage being 80 volts above the schematic and your pre amp plate voltages matching the schematic.
My statement concerned me using a 5Y3 in place of the GZ34, with the 125P2A, and seeing the pre-amp voltages in the range of the schematic.
Ahh yeah. Since it had the original bias resistor and tubes, that would have been a good number to haveThree other things that would be interesting:
1. Heater voltage
2. Output tube bias voltage.
3. Bias current/Pd.
Here some voltages from a freshly serviced 1961 6g3 using the original 125p17A and a GZ34 @117vac all original everything but E caps.
B+1 415vdc
B+3 356vdc
B+4 298vdc
V1P1 190 vdc (and yeah I know)